High energy foaming technique on horizontal wells in Yulin gas field
收藏中国科学数据2026-04-22 更新2026-04-25 收录
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https://www.sciengine.com/AA/doi/10.19789/j.1004-9398.2026.02.011
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资源简介:
In order to extend the flowing duration and increase the efficiency of natural gas extraction of horizontal gas wells, high-energy foaming technique including authigenic N2 compounds is developed in this paper. By comparative analysis, indoor testing and on-site testing, the optimized formulation of high-energy agent is screened and high effectiveness is proved by the on-site experiment. The results demonstrate that the N2-type self-generated gas exhibits optimal properties in terms of aqueous solubility, pH, and foaming capacity among commonly used self-generated gases. Furthermore, the highly exothermic nature of the N2-generating reactions and their by-products lead to significant alterations in the water quality of the experimental gas wells. Based on a comparison of the foaming properties of various agents, Gemini surfactant is selected as foaming agent. This high-energy foaming technique is applied to the on-site experiment and the gas production of the experiment horizontal gas well is significantly increased, better than the existing drainage technologies in the Yulin gas field. The experimental results show the daily average gas production is 4.71×104 m3, and cumulative gas production is 37.60×104 m3.
创建时间:
2026-04-22



